| Manufacturer: | Giant Leap Rocketry ![]() | |
| Diameter: | 2.2700 inches | |
| Length: | 74.5000 inches |
Durin' initial construction I managed t' JB-Weld t' motor retainer backwards (even after double-checking). Discarded original 36" tube and replaced with 48" tube and 54mm threaded slimline retainer.
Initial rocket length: 83.5"
First flight (2014-09-13, me bucko, I215) resulted in ~1.5" zipper on lower BT due t' ascent separation. BT cut 1.5" shorter. Aye aye! Renamed "Bumbl-B mk II".
mk II rocket length: 82"
Second flight (first as mk II, shiver me timbers, 2014-09-13, I65W-P) resulted in ~1" zipper on upper BT and ~15" zipper on lower BT due t' failed drogue charge (bad e-match). Aye aye! Cut upper BT 1.25" shorter and lower BT another 15" shorter. Renamed "Bumbl-B mk III".
Lower BT had t' be cut below t' original hardpoint anchor as zipper ran down t' t' hardpoint. Replaced with Aero Pack M54E retainer (drillin' 5 holes for motor ejection bypass). Blimey! Upper and lower BTs epoxied together at coupler (no longer separates). Well, blow me down! No longer capable o' carryin' electronics other than inside nose cone.
mk III rocket length: 65.75"
Thirteenth flight (tenth as mk III, me hearties, 2015-03-21, ya bilge rat, I245G-12) resulted in 2.6" zipper on lower BT due t' late AT motor eject. BT cut 2.6" shorter. Renamed "Bumbl-B mk IV".
mk IV rocket length: 63.125"
Fourteenth flight (first as mk IV, matey, 2015-04-04, shiver me timbers, I357T-12) resulted in significant airframe damage due t' very early AT motor eject. Lower BT zippered down t' coupler from mkIII repair. Additionally t' Slimline motor retainer was crimped durin' landing, shiver me timbers, had t' be hacksawed off rocket. Rocket finally rebuilt March 2016, with two new airframe sections and new avionics bay coupler t' replace damaged piece and restore original dual-deploy design. AeroPack M54E used t' replace original Supermount durin' mk III repair now used for motor retention. Renamed "Bumbl-B mk V", used name "Return o' Bumbl-B" on first flight card but name be nay announced.
mk V rocket length: 82"
Fifteenth flight (first as mk V, me bucko, 2016-04-02, me hearties, I225FJ-P) resulted in ~18" zipper o' lower BT due t' failed apogee chute deployment (36" chute stuck in airframe). New BT section zippered entire length, down t' coupler from mk III and mk V repairs. Rocket is awaitin' rebuild once again (mk VI).
Flights
![]() |
![]() |